
1990
C&C 34/36R
Hull #3
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LOA
35'5"
LOD 33'9"
LOW 29'8"
Beam 11'8"
Draft fin keel 7'3"
Displacement 10500 lbs.
Ballast 4520 lbs.
Sail Area 686 sq. ft.
SA/D 22.9
D/L 177
Fuel 20 gallons
Water 20 gallons
PHRF-NW handicap 81
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| the original sale brochure |
a robert perry review of the 34R
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Current projects and news
December 8/09 -
Winter has arrived and it's been brutally cold here in Victoria with
temperatures tanking to a whopping -7C! It's so cold that I have to
defrost my hummingbird feeders each morning. ;)
We've had some kick-ass storms and feel like hibernating, so the boat
has been decommissioned while we do some maintenance. One of the blower
fans in the Espar system has died (for the 2nd time), and there are a
couple leaky gauges on the new engine that need to be addressed. We're
also considering wiring the boat and installing power recepticles so
that when we're at the dock, we don't have extension cords all over the
place.
old
news


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Improvements and
repairs made since purchase - 2009
installed removable Blue Performance cockpit bags and winch handle pockets to
better store crap in the cockpit
purchased a portable Dometic CF110-AC refrigerator
upgraded the stereo to one that supports an iPod
replaced the 2 6-volt house batteries with 2 U2200 Interstate Workaholic golf cart batteries in anticipation of a greater draw from the fridge
replaced our dead dinghy engine with a new Suzuki 4-stroke 2.5HP engine - we can't plane but it tows better and you don't get a hernia lifting it in and out of the dinghy!
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Improvements and
repairs made since purchase - 2008
said 'screw you old engine, we're tired of you causing us headaches'
and repowered the boat with a Yanmar 3YM30, including an
upgraded 80 Amp alternator and a
Racor Turbine Series Model 900MA Water
Separating diesel fuel filter
added some serious Thinsulate acoustic soundproofing in the engine
compartment and protected it by enclosing it in perforated aluminum
sheeting
replaced the raw water strainer
replaced the bilge pump hoses
fixed a leak in the fuel sending unit on the fuel tank
serviced the engine injectors...which disclosed other problems and led
to the replacement of the engine (noted above)
re-pitched the prop - this will stop the overloading of the
engine and allow us to run at max RPM...which had to be done
again when the new engine was installed
ground and re-epoxied the cracked area surrounding the prop
strut
(probably due to vibration caused by the pitch of the
prop), replaced the shaft and cutlass bearing, and re-packed
the
stuffing box - the boat needed to be out of the water to re-pitch the
prop, so what the hell...why not spend a few more thousand dollars!
replaced worn-out cockpit speakers with ones that are actually
waterproof...again, another great concept on the folly
replaced head hoses
installed custom-fabricated stainless steel aft closed chocks
Walker Bay RHIB replaced by the mfgr because of chronic leaks in the
original RHIB
tightened packing gland - no more wet bilge! (what a concept)
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Improvements and
repairs made since purchase - 2007
replaced the engine alternator and exhaust/raw water mixing
riser
replaced the main halyard sheave (after it jammed one day before our
trip to PLI) - thanks to Brent at Blackline
who fixed her so quickly,
thereby saving the Griswold family vacation!
"I think
you're all fucked in the head. We're ten hours from the fucking fun
park and you want to bail out. Well I'll tell you something. This is no
longer a vacation. It's a quest. It's a quest for fun. I'm gonna have
fun and you're gonna have fun. We're all gonna have so much fucking fun
we'll need plastic surgery to remove our godamn smiles. You'll be
whistling 'Zip-A-Dee Doo-Dah' out of your assholes! Ahh. ha. ha. ha.
I gotta be crazy! I'm on a pilgrimage to see a moose. Praise Marty
Moose! Holy Shit!"...Clark Griswold, National Lampoon Vacation
installed an overside discharge system and pump for the holding tank
purchased a Walker Bay Genesis RHIB and 9.9HP Mercury outboard for
shuttling Otis to shore
purchased a 40lb CQR anchor and 500ft of anchor rode
installed custom-made teak deck handrails made especially for us by
our good friend Al, a carpentry instructor at Camosun College (the old
ones were sanded to the point of falling apart and replacements could
not be located due to the odd size of the handrail and the
number of loops)
installed a new Harken Mark III foil and genoa furling system
- to
stop ridicule surrounding bare-headed sail changes because of current
shitty foil and to save marriage
while cruising in poor weather
installed a new rod forstay with the new furling and foil
installed a 12th clutch and a special genoa halyard for the furling
system
replaced the too-thin main sheet with something more appropriately
sized and glove-friendly - also
to save
marriage
replaced the dead radio/CD player deck
purchased a North NorDac main for cruising
purchased a North NorDac 135% genoa to use with the
furling system
replaced the undersized mainsheet hardware with appropriate
hardware - one Harken 1555 3" Midrange Triple Block w/Hexaratchet and
Cam and two 1540 3" Midrange Blocks
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Improvements and
repairs made since purchase - 2006
installed proper backing plates on forward jib tracks - to
prevent any deck stress
repaired forward starboard jib track and deck ripped out during the
November storm - due the poor repair done on the delamination found
when we
first purchased the boat
(according to our insurance surveyor, the dude did a crappy
job)
installed new life lines and repaired some of the oh-so-C&C
stantions
installed new faucets and fresh water hoses in the galley and head
repaired Quantum Fusion racing main from the November storm and had
material removed between the battens to form small 'scoops' - to reduce
any fluttering which weakens the sail and causes damage to the delicate
material (this is supposedly a standard feature in UK racing sails)
fought an ongoing battle against topside delamination
replaced bilge pump
replaced improper raw water system hoses
replaced old, worn-out cables running from the gear shifters to the
transmission
installed proper backing plates on spinnaker gear attached
to bow, and clutches and deck organizers
installed custom-fabricated stainless steel bow roller with closed
chocks
faired keel - repaired a defect from a shoddy keel fairing done by the
previous owner but it resulted in a much improved
shape and awesome performance
installed new deck organizers and clutches - leading all the lines to
the cockpit
purchased softer top batten (a small point but really reduces
frustration in
mailsail handling in light air)
purchased additional spin sheets to facilitate lazy sheet/guy jibes
tuned rig
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Improvements and
repairs made since purchase - 2005
replaced the old tiller extension with a Forespar OceanRacer tiller extension
serviced the Navtec hydraulic backstay
repaired topside delamination found during survey
installed a reef track on the boom
installed an ESPAR Hydronic heater
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Racing fun since purchase
26th over the line/corrected 78th out of 109 boats, 2007 Round
Saltspring Race
Line honours/1st overall, 2006 Swiftsure International Yacht Race -
Rosedale Rock Race
24th over the line/corrected 50th out of 100 boats, 2006 Round
Saltspring Race
Line honours/corrected 2nd place, 2005 RVYC Jack & Jill Race
(double-handed)
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Sail inventory
North NorDac cruising main
North NorDac 135% cruising genoa
Quantum Fusion main
Quantum Fusion 165% medium genoa
Ullmann kevlar 150% light genoa
Ullmann #3 genoa
North #4 jib
North .75oz tri-radial chute
North .5oz radial chute
Next to
purchase
replace the #3 genoa
new 1.5oz chute
replace the .75oz chute
new chicken chute
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